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  • experimental simulation investigation of diaphragm rupture and washing for rocket engine in arc heated air flow

    Paper number

    IAC-15,C4,IP,11,x27989

    Author

    Mrs. Cheng Meisha, CASC, China

    Coauthor

    Prof. Lianzhong Chen, China Academy of Aerospace Aerodynamics, China

    Year

    2015

    Abstract
    To check the rocket engine diaphragm rupture state under certain differential pressure when the rocket engine begins igniting and to study the diaphragm state as enduring long time washing in high temperature air flow field, based on the arc heater test facility, the special pipe test simulation system has been developed, and the natural deficiency of diaphragm rupture happening in advance during the cold air supplied to arc heater before ignition has been resolved. Using this system, the diaphragm rupture process in thermal air flow has been successfully simulated, and the diaphragm long time enduring washing reliability in the high temperature air flow has been proved. The results provides guarantee for the successful rocket launch.
    Abstract document

    IAC-15,C4,IP,11,x27989.brief.pdf

    Manuscript document

    IAC-15,C4,IP,11,x27989.pdf (🔒 authorized access only).

    To get the manuscript, please contact IAF Secretariat.